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HEIDENHAIN TNC7 Handleiding pagina 2838

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41
Foutnummer
237-180BD
237-180BE
237-18500
2838
Beschrijving
Error message
180BD Position monitoring for field-angle adjustment %1, ES
%4
Cause of error
- The maximum position deviation was exceeded during the
field angle adjustment.
The additional information indicates the active emergen-
cy-stop input, if set:
0 = No emergency-stop input is set
1 = Emergency Stop A
2 = Emergency Stop A Handwheel
3 = Emergency Stop B
4 = Emergency Stop B Handwheel
5 = Emergency Stop B Functional Safety
6 = Emergency Stop B Functional Safety Handwheel
7 = Emergency Stop A Functional Safety
8 = Emergency Stop A Functional Safety Handwheel
Error correction
- Check the parameter CfgControllerAuxil > chkPosHoldFiel-
dAdj and increase it, if necessary
- Check the external wiring, especially the emergency-stop
inputs
- Check the encoder and motor data
Error message
180BE Monitoring of servo lag inactive %1
Cause of error
- The parameter CfgPosControl > servoLagMax2 has the
value 0
- Only for spindles is it possible to deactivate servo-lag
monitoring.
This is not permitted for axes.
Error correction
- Set CfgPosControl > servoLagMax2 to a value greater than
0
Error message
18500 SKERN-CC%2: Meetsysteemfout CRC X%4
Cause of error
- Checksumfout bij de meetsysteemgegevens
Error correction
- Reboot van de besturing
- Regeleenheid (CC of UEC) eventueel vervangen
- Neem contact op met uw servicedienst
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HEIDENHAIN | TNC7 | TNCguide | 01/2022

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